Chris Hammond
Tuesday, August 07, 2007 6:51:57 AM
Tonight I told myself I wouldn't start the car, I would get ready for my trip to Chicago tomorrow (going up there to give two days of DotNetNuke training classes).
But I couldn't help myself, I had to get the camera and record the new exhaust! It's not quiet, but oh it sounds so sweet!
Here's a 2mb WAV file of the car running
Here's a large WMV video of the same...
Views: 1121
Chris Hammond
Tuesday, August 07, 2007 1:20:24 AM
So it's been over a week now since I drove the 240Z for the first time. What have I gotten done in that timeframe? Not much!
I basically didn't touch the car until Thursday, and all I did then was take a few minutes to inaccurately measure the requirements for the flange on the downpipe. Friday I picked up a header collector flange from my buddy Russ' place. Sunday morning I went to work on that flange, it needed some help to make it fit.
Sunday afternoon I spent some time in the sauna, I mean garage. I managed to get the coil pack and EDIS module mounted to the fender. I then started trying to clean up some of the wiring in the engine bay. I got some plastic loom a while back so I started running that to cover up the mess of wiring in the engine bay. I also ran the loom in the passenger compartment around some of the wiring in there. It's not finished, but it's definitely starting to look better.
Dad helped me to put a switch inline for the main relay. Luckily with the car not idling yet I haven't had problems turning the car off, but with the way things were wired if the car was idling properly you'd have to pull a fuse or disconnect the battery to shut off the car. Now that I have a switch it's easy to do!
After that Dad and I put the hood and hinges on the car, the first time since I've owned the 240 that it has had a hood attached! From there we loaded the car up onto the trailer later in the evening.
This morning I got up early (a rarity for me) and took the car/trailer over to the Carx on St. Charles Rock Road in Bridgeton. Rick was extremely helpful over there and by 12pm today I was back up there loading the car up on the trailer with Eric's help. Carx put a 3" pipe from the downpipe back to the rear axle, with a turndown on the end.
It's still quite loud, but if I do say so myself, it sounds pretty damn sweet! Eric and I brought the car home, and before trying to push it off the trailer I finally got it started. I'm having starter issues and will probably try to replace the starter Thursday or Friday of this week.
I drove the car off the trailer and into the garage, it's a beautiful sound!
I'm still aiming to compete drive the car at the Autocross on Sunday. Before I can do that I have quite a bit left to do.
1. Fix the idle (longer idle screw)
2. See if there's any fluid in the transmission (can't get the fill plug out so I've not pulled the drain plug yet)
3. Build a bulkhead/firewall for the fuel cell
4. Finish up wiring for the O2 sensor
5. Get a harness squared away
6. More stuff I'm sure I've...
Views: 885
Chris Hammond
Wednesday, August 01, 2007 1:10:41 AM
Thanks to everyone who helped on the car I was able to tow it out to Gateway yesterday for the SCCA Autocross. I didn't plan to compete the car, but I brought everything with me that I needed to get it put together enough to try driving it for the first time.
After I installed the driver's seat with the help of Phil Cline, Whittle and I bled the brakes on the car. From there it was a matter of hooking everything up and getting her off the trailer. Below is the link to the video page, thanks to Dave for filming the first drive.
First Drive Video
I can't thank everyone who has helped me get this far enough. I'm far from done with the project, but the biggest hurdle in my mind has been cleared. My biggest fear was that once together the car just wouldn't run, and now it runs!
Thanks to the following, in no particular order:
Russ Melton
Dave Whitworth
Eric MacKenzie
Terec Willson
Andy Whittle
Andy Hohl
Bill Hammond (my dad)
Ronnie Baker
Henry Kenuam
Everyone of those guys' wives!
And of course my wife Natalie for letting me spend the past few months dirty and greasy!
This will most definitely not be the end of the project, just the beginning of a running car!
Edit: I knew i'd forget someone! Thanks to Mark and John Huebbe for the use of the welder, and inspiration of the...
Views: 978
Chris Hammond
Sunday, July 29, 2007 8:55:17 AM
That's right, it runs!!!! More info tomorrow, I've gotta get up in 5.5 hours for the autocross tomorrow!
Here's the video page, crappy video and sound, but it does...
Views: 1000
Chris Hammond
Saturday, July 28, 2007 10:10:17 AM
This morning I woke up with a little hope in my eye, hope that I would make some good progress today.
After doing some reading online about the Megasquirt and Edis I headed out to the garage. The first thing I noticed was that the coil pack wasn't plugged into the Edis module. I'm not sure if I had unplugged it last night when trying to figure out why we didn't have any spark, or if I hadn't plugged it in at all last night.
I then hooked up the laptop and tried to start the car, to see if anything changed. At first nothing was different than last night, no spark and no RPM signal on the squirt. But a few tries later I noticed the RPM on the laptop jumped up. Sporadically I was able to get RPM but nothing consistant or worth a darn from a starting perspective.
I decided from there I would need to mount the coil pack and the edis module as I hadn't mounted them yet, they were just laying in the car. To do that I needed to pick up some metal as I didn't have enough to fabricate much.
I headed out around noon to the DMV, it was time to get the trailer registered, and then head to Illinois to pickup the trailer, fix the wiring on the trailer, and then hit Home Depot on the way home to pick up the metal. The trailer pickup took far longer than I expected, but with the help of Andy and Chris Hohl I was able to get the wiring on the trailer fixed!
When I got home I backed the trailer into the driveway and got to work on the car again. Before I went ahead and started building brackets for the EDIS setup I decided to try and rewire the VR sensor on the car, to see if that might fix my problems. I checked a few things I had lying around. I had a VR sensor for a V6 Ford Explorer, but I was using the VR sensor that matched the 36-1 wheel off a 4Cylinder Escort that I had mounted to the car. I checked the wiring on both sensors and noticed that the colors were opposite on the Explorer plug.
After swapping out the VR sensor wires I went to fire the car up, sure enough I had a full RPM signal on the laptop! Score! I then started checking to see if I had any spark. Eric showed up and we weren't getting any spark. To try something out we plugged in the other coil pack and hooked up one wire/plug sitting on top of the valve cover. Once we did this we immediately noticed spark! Score again! Just to see if we had something else wrong we plugged back into the original coil pack, and sure enough this one also sparked. One thing we did to the original coil pack was to run a wire from one of the mounting points to the shock tower on the passenger side.
I'm not exactly sure what changed to cause us to start getting a spark, but I think it most likely related to this ground, perhaps, I'll test it out again tomorrow without the ground and see what happens.
Once we had spark we hooked the fuel pump back up and tried to get her to fire. First thing we started getting was a few pops and then lots of smoke! Score again! After a few attempted we decided we'd tried enough for the time being. Eric headed out and I decided I needed to try something else. I remembered reading today that the EDIS coil pack should run 132, and we had plugged in the wires for 123, so I swapped this around.
As soon as I attempted to start it was a totally different sound, it was beautiful! I've not yet gotten it to start, but it sure sounds like it's trying to. I had Andy Whittle on the phone throughout the night and I sent him a few log files from the data I recorded while trying to start the motor.
Around 10pm I figured it was probably a little too late to try to keep starting the car with all the noise it was creating. I got under the car and hooked up the speedometer cable, put the missing bushings into the transmission crossmember and tightened that up as well as the clutch slave cylinder.
I've got a few things to try in the morning before I head off to the muffler shop to see if I can't get an exhaust put on the car.
Here's some video from tonight, trying to...
Views: 644
Chris Hammond
Friday, July 27, 2007 10:31:04 AM
First off, let me say that today was a good day! It didn't start off that way however. After last night's fuel rail issues I needed to get the rail tapped and get myself a new fitting. At lunch I headed over to SoloPerformance World Headquarters to have Dave assist with tapping the rail. He didn't have a 3/8 NPT tap so I had to head over to Grainger down the street from the SPS offices and pick up a tap. $33 later I was in business and heading back to Dave's. He assisted with tapping the rail again and then I headed south.
I needed to go to SCPRacingparts.com to pickup another fitting, they had just what I needed and then I was headed back to the office. When I got home this evening the first thing I did was check to see if the new fitting would be what I needed. I put the fitting into the rail with some teflon and hooked everything up. I pressurized the fuel system, and sure enough, it was leaking fuel again! Not a happy camper was I. With a leaking fuel rail I couldn't do much else so I called up Speed Sports to see if they could help me out by tapping the rail and selling me a new fitting.
They were running a little late and not open yet so I decided to work on the power issue we were having with the Megasquirt. On Tuesday we had problems because the MS signal to the laptop was highly unsteady. We weren't sure if it was a power problem, or if it was related to a bad ground. Tonight I replaced the wire we were running to the main relay with a direct line from the battery. Once I did this the relay kicks in immediately when plugged to the battery, powering up the megasquirt without the ignition being on.
This corrected the fluctuation issue, which was great news! Now that the gauges and sensors seem to work fuel was the last major hurdle before I could attempt to start the car. I headed up to Speed Sports and had Lou tap the rail and install a new fitting for me. He showed me that I wasn't using enough teflon on the fitting, and he also managed to run the fitting nearly all the way in, where we were only able to get it in a few threads before.
Once I had the new fitting installed I was starting to get excited, perhaps it would hold and I'd be able to see what happens when I cranked the car. Installation of the rail was easy, I've installed and removed it so much in the past two nights that it is easy to do now. Eric showed up and we pressurized the fuel system a few times. All tests appeared good, no fuel leaking out anywhere!
Now it was time, the power was good, the fuel was good, it was time to try and start the car. Eric and I tied up a few last minute things, hooked up the battery, computer to the Megasquirt and watched all the gauges on the PC light up. Eric stood by the front of the car with a fire extinguisher and I reached into the driver's door to turn the key.
I turned the key, she cranked over, a beautiful sound I must say. After a few cranks I realized the fuel pump wasn't running, which meant that the squirt wasn't getting an RPM signal as it should be. I looked over at the display and sure enough, no RPMs registering on the PC. Without RPMs the Megasquirt won't allow the fuel pump to run for more than 2 seconds, that was my giveaway.
I called Whittle up and he suggested a few things. First thing was to pull a spark plug and see if we were getting any spark. Nothing. Then I checked to make sure the EDIS was getting power, it was.
So that's where I'm at right now. I've got a bit to do tomorrow, I need to diagnose why I'm not getting spark. I'll check a few things first, see if perhaps the VR sensor is wired backwards, which would cause this. I'll also check to make sure I have the VR sensor in the correct location. I'm taking off from work tomorrow to try and finish things up on the car this weekend so I can race on Sunday. We'll see if I reach my goal!
Overall I was very pleased with the progress tonight, even if the car didn't start I gave it a shot,...
Views: 693
Chris Hammond
Friday, July 27, 2007 9:53:11 AM
Well, Wednesday night was an eventful night. When I got home from work I jumped under the car and tried to track down my coolant leak. I found small traces of coolant here and there, but I didn't find any big problems. While under the car I found a few other things. I noticed that the oil return line off the bottom of the turbo wasn't hooked up. Thankfully I found that, had I tried to start the car with that disconnected we would of had a real mess on our hands.
I found the coolant leak I was looking for, it, like the first coolant leak we found on Tuesday night, was in the thermostat housing. There was a plug in the housing that hadn't been covered in teflon and hadn't been tightened down enough either. After that I started to hookup the vacuum lines for the wastegate to the turbo.
Once I had finished under the car I decided it was time to track down the fuel leak in the rail. We initially though that the first 3 injectors were leaking on the rail, so I spent an hour notching the fuel rail brackets so that I could lower the rail close to the intake manifold more, adjusting the angle of the injectors. This ended up not being the cause of the leak, but I do believe that the angle of the injectors is now much better than before as they sit in the rail and intake much better now.
The cause of the fuel leak ended up being the 45 degree fitting we had on the inlet end of the rail. When removing the fitting on the rail I found that both the threads on the fitting and the rail were bunged up really good. There was no reusing the fitting so I would have to get another one and retap the rail.
Here's the video I took of the work...
Views: 627
Chris Hammond
Wednesday, July 25, 2007 11:30:59 AM
Fuel leaks, coolant leaks and blown fuses. That about sums up the evening...
First off, a HUGE thanks to everyone who came over tonight. Henry, Ronnie, Terec, Ian, Eric, Scott and Andy, without you guys helping out I wouldn't have gotten anything done tonight!
Here's a basic summary of how things went tonight. Henry and Ronnie showed up first and got to work on finishing the wiring in the engine bay. They by far did the most, if not all of the work on the wiring on the car, I had put together three wires, but they as a team crank though some things, far faster that I could ever hope to.
While they spent time working on the wiring in the engine bay I did a little work in the passenger compartment trying to get some wires run, finding parts for them, and trying to close up some ports on the intake before the turbo but after the MAF.
Before heading to the interior to do wiring Henry, Ronnie and I attempted to crank the starter, to see if it would fire. Because this car is now a manual, but originally was an auto Ronnie wired up a relay to bypass the neutral safety switch that keeps the starter from firing if the car isn't in park. We were unable to locate the stock relay but found some of the wiring so we just ended up bypassing the whole thing.
When they were working on the interior wiring I finished up some of the engine mount bolts that needed tightening and started cleaning up the Ford plug wires that I had picked up from the junk yard a while back.
The rest of the guys started showing up, when Whittle called me I told him we were about half an hour from trying to start the car, he's the megasquirt Guru so I asked him to come over and assist us with things while we tried. By the time he arrived we weren't quite ready, but we thought we were close.
Once the Whittle's showed up we ran some fuel through the fuel system into a jug (rather than the fuel rail) to try and clean out the hoses and pump, to keep any buildup from getting into the rail and injectors. That testing went fine, but as soon as we hooked the fuel lines back up and sent some pressure through the system we found a few leaks. The fittings at the fuel filter in the engine bay had been put together without teflon, lesson learned, 10 minutes later it was all back together again and pressure testing started up. Then we found a bigger issue, but one that didn't dump near as much fuel out. We can't seem to get the injector for the number 1 cylinder sealed into the fuel rail, it looks like the 2 and 3 injectors are also leaking a bit. So, tomorrow, the fuel rail will come off and we'll try to make adjustments.
On the electrical side of things: At first we couldn't get the MS to fire up at all with the power from the car. After about 15 minutes, and Whittle about to give up I started looking for wires and remembered, we ran the TPS and TPS Signal wires, but don't currently have a TPS to hook up to, well sure enough, they were sitting right on the intake manifold. As soon as I removed them the Squirt fired up in Megatune. Then there were a few other gremlins. The MS seemed to be getting power spikes, though not completely resetting itself and firing the fuel pump again.
At first we thought this was a grounding issue, but I believe I've now tracked it down just to be a source issue. While trying to track that down we started blowing fuses in the stock wiring. We couldn't figure out what that was happening until I looked at what we had wired into for the switched power line. I found that we were jumped into a line for the AC, well two days ago I pulled the AC system from under the dash and the wiring was still there, half hanging out of the car, which of course was touching the chassis, and causing out problem. Once I figured that out I removed the AC wire from the equation. That corrected the fuse issue, but we're still getting the power fluctuations, so I'll be tracking those down by checking...
Views: 542
Chris Hammond
Tuesday, July 24, 2007 10:41:14 PM
As of right now, the goal for tonight is to attempt to start the...
Views: 647
Chris Hammond
Tuesday, July 24, 2007 9:36:36 AM
Today was a good day! Progress was made! First things first, at lunch myself, Henry, and Eric headed down to High Ridge to SCPRacingparts.com again to get a cap for my Fuel cell, I realized yesterday that I was only 3 of the 4 fitting points for the fuel cell, and I had better get something to cover the fourth one up.
After work my Henry (one of my bosses) and his mechanic buddy Ronnie came over to the house, after we made a quick pitstop at Gateway Electronics again to get more wiring items (I also spotted the Rally Bug builders on their way home from work). Ronny runs a shop down south near where he and Henry both live, so he was an EXCELLENT resource to have working on the car tonight. He and Henry got nearly every wire in the engine bay connected and placed in the appropriate areas, leaving just a few things for me to do in the bay.
Eric also came over after making a trip to Autozone to get the battery for his 3rd gen RX-7 recharged. He finished up the fuel cell items that needed done. Adding the inline filter before the pump and then attached the vent line with the bulkhead fitting and check valve.
I spent the evening doing minor things, mainly being in awe of all the work that Henry and Ronnie were getting done. I did track down some keys to the car, though I swear the keys I grabbed were the keys to the parts car I got rid of, one of them fit into the ignition for the 240z. I also figured out that the ignition has been turned on this whole time, which would explain why we never needed a key to turn the steering wheel when rolling the car around, though I'm not sure how it was turned on and the key removed. I do have the ignition out of the 78, as well as the turn signal and headlight switches from that car to try and use on the 73.
Ronnie was able to get the power from the new battery hooked up to the starter, and alternator, which in turn got power to quite a bit of the car. One of the hazards work, the parking lights looked to work as when the headlights were turned on the rear lights lit up. I'll ahve to figure out how to wire up the headlights in the future, but I'm guessing the wiring for them should be somewhat intact based on testing tonight.
So I've got more work to do tomorrow night. I'll try to finish up the wiring that is left in the engine bay, as well as wire up the fuse panel and try to mount the Megasquirt tomorrow night.
Right now my goal is to try and start the car either Wednesday, or Thursday night! Though, I'm seriously thinking I won't be going to Topeka, though I'm still hoping to at take the car to the local autox this...
Views: 539
Chris Hammond
Monday, July 23, 2007 10:34:20 AM
Here's a quick update on the 240. I got up this morning and finished up modifications to the bracket I built for the VR sensor, you can see what it ended up looking like in the photo below. It's not all that pretty, but not too bad considering I made it out of a drill press, vertical sander, and a jig saw.
I then ran out and spent a few more hours shopping. I went to autozone and purchased lots of random bits that I needed, another fuel filter (that didn't fit), wires, splices, antifreeze, radiator hose, oil, gear lube, and a ton of other random stuff. I also took the battery I had purchased for the parts car back to get tested, it wouldn't charge so they gave me a credit (it was out of the year's free replacement), so I got a new battery for $9.95.
Whittle came over and assisted with a few more wiring questions. From there I tried to get started on wiring. I began by looking where exactly I was going to run the wires, in order to find an existing hole to run them through I got up under the dash and started removing things on the passenger side. The first thing I removed ended up being part of the AC system, which I wasn't actually sure the car had! That opened up two holes, with grommets to boot, that allowed me to start running wires.
Terec came over and started assisting with a few things, first thing we did when he got there was make a list of all the tasks left to do on the car. We used a sharpie on the windshield. After that he was visibly more productive today than I was. He actually mounted the sensor up to the motor and made sure that it was within specs to the 36-1 wheel. After that he was able to get the radiator mounted and the hoses attached to the proper locations. He then got the Oil Cooler mounted and the hoses finished up from what Eric started doing yesterday. You can see the oil cooler and radiator mounted in this photo.
I was able to get some of the EDIS wiring started, as well as power wires ran for both injector banks, as well as the Megasquirt harness wired into the engine bay, though the MS harness doesn't actually connect to anything yet. I have a LOT more wiring to do this week, hopefully getting most of it done Monday and Tuesday night with a goal of trying to start the car on Wednesday. We'll see if that happens, if I don't at least attempt to start it before Sunday I've vowed to shave my head....
Here are more photos from today.
...
Views: 570
Chris Hammond
Monday, July 23, 2007 10:33:54 AM
Eric and I got a bit done today. Mostly learning with the help of Andy Whittle who stopped by to assist with some Megasquirt questions. I also did some soldering on the Megasquirt wiring, LOTS more soldering to do tomorrow!
The fuel cell is mounted, Eric started on the oil cooler mounting, we ended up figuring out that I did have the correct peices for that, so all that money isn't wasted.
Sunday tasks
Connect Fuel Lines
Run Megasquirt Wires, Fuses, Relays
Install Megasquirt
Install Fuse Panel
Install Battery (charge battery)
Install Seats
Install Radiator
Connect Starter
Connect Alternator
Add Oil to the Motor and Transmission
Add Coolant
I'm sure I'll have to add more to this...
Views: 609
Chris Hammond
Saturday, July 21, 2007 10:12:38 AM
Today we made some good progress. Mark helped me at the office today to solder some more wiring for the megasquirt. I've still got a LOT more wiring to do, but that part of things is starting to come together.
Tonight I finished up welding for the VR sensor bracket and then Eric came over and we spent time connecting things in the engine bay. We have more of the fuel lines connect, oil feed for the turbo, and other things going now. I've got a few fittings to purchase Saturday morning, a few bolts to purchase, and grommets to fill some holes.
Saturday morning I'll be up early, running around for a few parts, then back home to finish up the fuel hardware. I'll start on running wires for the megasquirt tomorrow morning.
Mostly, after the fuel lines are taken care of, I just have electrical things to work on. Any EE's out there who want to come play...
Views: 612
Chris Hammond
Saturday, July 21, 2007 12:30:00 AM
After work last night I got to work on the car. Eric and Russ came over to lend their assistance as well. Russ got started on the leaking wheel cylinder, Eric started putting the Intake/exhaust/turbo back onto the motor, while I worked on fabricating a bracket to mount the VR sensor onto the side of the motor.
While they were both productive, I actually never got my portion of the project finished last night, though I hope to finish it up tonight. Once the intake/exhaust and turbo was all back together we went ahead and began the task of putting the motor back in the car. I've got some High Definition video of that process here on this Video Page.
With Eric and Russ' help we also managed to get the drive shaft connected up and the transmission into the cross member under the tunnel. Tonight I'm going to pick up more bolts, so we can mount the fuel cell bracket to the floor of the car and then we can hookup all the fuel lines. We'll also be installing the fuel rail and injectors tonight so we can hook up the fuel lined up front.
At that point I hope to start trying to figure out the wiring for the car, that's the big project left for this weekend, get wiring going so we can try to start this bad boy up.
Here are some various photos from last night
...
Views: 525
Chris Hammond
Thursday, July 19, 2007 9:14:00 AM
Tonight Natalie and I went and looked at a house, it's got ~5 acres, a 2 stall barn, a hay shed, and an oversized two car garage. That covers the basics. While looking around in the garage I found a circuit breaker, sweet, setup just for the garage. It's even got a section marked "Welder"! score, 220 already wired in the garage. Where do I sign?
I got home and finished dinner around 9 or 9:30pm, didn't feel much like working on the car. So, I didn't. Then I thought, well I had better check if the fittings I ordered last night would work on the oil cooler adapter. Guess what? They don't f'ng fit! I don't know who was smoking crack on the HybridZ Forums, but the oil cooler adapter plate's fittings are NOT 18mm, at least the 18mm x 1.5 to 10AN fittings I got sure are too damn big.
After I found that, all the stuff I had overnighted from Summit last night is pretty much useless, at least until I figure out what sizes I really need, or I just try to order another oil cooler adapter. That set me over the edge, I decided I was just going to try and take the oil filter adapter out of the block from my 78 280Z motor sitting on the floor of the garage.
The other night I attempted to find two nuts to fit over this to aid in backing this adapter out, I failed at finding any. So I took my vice grips and clamped down, the adapter came out rather easily. I stuck that adapter into the block on the turbo motor, and stuck the oil filter on. Problem solved, no more oil cooler, at least not for now. Though I could have saved myself a few hundred bucks had I just done that two nights ago :(
Later tonight I went back out to the garage (around 11:30) and started looking at how I'm going to fabricate my mount for the VR sensor to read the 36-1 wheel. I think I have a good setup figured out and will fabricate that immediately after work tomorrow so I can try to finish up any welding I may need to do (I think that's the last thing) because I know the Rally Bug will be needing the welder back...
Views: 590
Chris Hammond
Wednesday, July 18, 2007 9:32:53 AM
Monday night I didn't get crap done on the project! I started to work on the oil filter/block attachment only to realize after driving around for 2 hours that I wasn't going to find any easy way to block off the oil cooler attachments for the 83 L28ET motor. By the time I got home from that it was well after 9 and I needed to spend some time with my wife.
Tuesday I ordered AN fittings to go from the metric 18mm x 1.5 oil cooler fittings to AN -10 fittings so that I can run steel braided lines to the new oil cooler I ordered. All of that should be here tomorrow.
Tuesday after work I began putting things back together on the Intake Manifold. I spent far too long digging around the garage trying to find parts I haven't seen in a few weeks. Yes, I need FAR BETTER organization in the garage. I'll probably have to spend some time Thursday or Friday night cleaning up if I'm going to have anyone over to help out this weekend. After that I headed off to Speed Sports up in Bridgeton (http://www.speedsportstopfuel.com, store hours from 7-10pm M-F) to pick up some AN-4 steel braided line for my turbo oil feed. I got a 1/8" NPT to AN-4 fitting, a 90 degree hose fitting, and the fittings I needed on the turbo side, as well as 5 feet (about 1 ft too much) of AN -4 hose. I figured out when I got home that the port on the block for the oil fitting is NOT 1/8" NPT, it's actually 1/8" BSPT, which is very similiar, but different enough to make my fitting not work.
With this info, I think I've now figured out why the pipe thread plugs I had purchased a few months ago wouldn't work, I probably need BSPT for those as well. I've found a few parts online that I can order to convert from BSPT to NPT, I'll see if anyone locally has those tomorrow, otherwise I'll get those ordered tomorrow.
After leaving Speed Sports I headed down the street to Autozone. At AZ I picked up a lot of hoses, clamps and other random bits of things I needed to reassemble the motor. I also picked up a GM open element Air Temperature sensor to thread into the Intake manifold to be able to tell what the air temp is going into the motor, I had to get the Wells part, I think SU107 was the # but I could be wrong. AZ didn't have a pigtail so I'll try Carquest tomorrow to see if they have the pigtail so I can wire this up to the megasquirt.
When I got home I threaded the temperature sensor into the Intake manifold. I also managed to get the thermostat gasket installed into the housing, the GM Water Temperature Sensor installed into the Thermo housing, and cleaned up the snail for the turbo. It was a bit dirty from sitting in a barn for who knows how many years. I'll take pics of everything later this week.
After running around this evening I got to thinking about how much this project has cost me lately. Without going into specifics (because my mother will read this) I've spent more this month than I spent to purchase the car. June was the same, and possibly double what I've spent so far this month.
I know I've got a few more things I'll have to purchase, but hopefully I've got all the big items out of the way, at least for this phase of the project.
More coming this week, and I promise to start doing video...
Views: 586
Chris Hammond
Monday, July 16, 2007 9:14:37 AM
After yesterday's fun Eric and I spent some time in the garage today. I was awoken this morning around 8:00am by the doorbell, the Dish Network guy showed up right on time, more on that topic tomorrow on http://TheMadBlogger.org. After I got the Dish guy going I sent Eric an SMS to let him know I was out in the garage working.
The first thing I need was to lay some fiberglass in the passenger floorboard. I had missed a few spots on that side earlier in the week, and layed some extra resin in the floor to smooth out the pockmarks from the cleaned up rust.
While I let that dry I pulled the extra rear end that I had in the garage so I could start cleaning it up. As soon as I saw the rear end/suspension sitting in the driveway I immediately noticed a difference from the rear suspension that is on the car currently. The current suspension doesn't have a rear sway bar, the spare does. That's fine and dandy, I'd prefer the rear sway bar, the problem though is that the fuel cell frame that I fabricated fits right where the sway bar goes on this spare suspension.
I'm not sure what I'll do with that aspect, but Eric and I spent the rest of the morning taking apart the spare rear suspension. We cleaned a lot of parts, figured out that the shocks (at least on the rear) are KYB's, they do look to be fairly new (or unused as that may be more correct). We got just about everything apart, and came up with plenty of parts to clean and paint (Powdercoat for Rande?) later in the project. Before I can use the rear swaybar I'm going to have to figure out what I'll need to change on the fuel cell bracket to make it work. I might be able to move the mounts for the bar a little higher to allow me to use the cell as currently fabricated.
From there Eric and I started to prep for paint the interior. We cleaned up some of the dust that had gathered, drilled some pilot holes for the seat bolts in the floor (to get to the rear brackets for the seat mounts we had to cut a whole for a socket to fit through). We brushed, vacuumed, wiped and scrubbed the interior to try to get it ready for paint. We lowered the car down off the jackstands and spent the rest of the afternoon painting the interior with a nice satin black "Chassis Saver" paint that I had picked up on Saturday morning.
I had purchased a gravity fed spray gun back in 2003 when I had the 350Z, previously using it once to spray some waste of money wax on the car, the gun hadn't been used since then. I think the paint this time around turned out great, an easy low cost solution that is WAY cleaner than it was prior to all this work. It was a bit laborious, but I think well worth the effort, Eric agrees.
Here are some before pictures
And here are some after shots.
There are more photos in my Flickr set for Project240z.com
We ended up painting a few coats over most areas of the interior and then let the car sit for a while to dry. Once dry we rolled the car back into the garage and started running fuel lines. We ran both the feed and return lines for the fuel cell, mounted the pump again after removing it for paint, and fixed the fuel lines to the transmission tunnel.
Tomorrow I'll be working on the motor again. I hope to get the intake and exhaust manifolds back on the motor so that we can put it in the car Tuesday or Wednesday night. From there it'll be time to start wiring up the...
Views: 614
Chris Hammond
Sunday, July 15, 2007 8:25:28 AM
Well, I got absolutely nothing done on the car today. I did manage to buy a few necessary items, but work on the car was not had.
Instead I spent the day helping my buddy Eric. He mistakenly LOST his girlfriend's parrot last night. So today we went bird hunting all day. Finally around 7pm Kendra stepped up and showed she had a bigger pair than both Eric or I. She climbed a tree about 3-4 stories up and got the bird to come down to her.
A more detailed blog post will be on http://chrishammond.com later this...
Views: 619
Chris Hammond
Thursday, July 12, 2007 9:00:59 AM
Tonight I spent some time working with fiberglass in the car. I was hoping to repair a few of the holes in the floorboards.
I made quite a mess, but learned quite a bit. Here are some before photos.
The passenger side needed the most work as it was in the worst shape due to rust. I used quite a few pieces of fiberglass matt on the passenger floorboard covering some of the holes. I also covered up a few of the sharper metal pieces of the floorboard.
On the driver's side I used minimal fiberglass matting and mainly used resin. The driver's side was in far better shape than the passenger side so I used resin to smooth out the surface on the driver's side. It turned out far better than I could have imagined! You can't really see it in the photos, but it's quite a clean look on the driver's side now. I can't wait to see how all this looks once painted. Though before I paint I'll be cleaning up the fiberglass with some sand paper.
I'll spend some time Thursday and Friday night working on the floor. I hope to try to paint the interior this weekend. The interior may have to wait though as I hope to finish up a few other things this weekend, mainly the fuel lines and getting the motor back into the...
Views: 563
Chris Hammond
Tuesday, July 10, 2007 9:14:41 AM
I spent some time this evening working on the interior of the car again. I went through one wire wheel and halfway through another on the passenger side of the car tonight.
Tomorrow I'll be doing some final prep work, possibly laying some fiberglass (for the first time) and then later this week painting the floor.
Photos and more later this...
Views: 820